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1B. Vallance and 1T. Adamus
Contact: vallanceb@ae.ca
adamust@ae.ca
1Associated Engineering, Calgary, Alberta
ABSTRACT
The NOVA Chemicals Plant at Joffre, Alberta is undergoing an expansion
of its production facilities. The expansion will require upgrading the
site's water supply and treatment and wastewater handling systems.
The Red Deer River is the source of water used on site. The main demand
for water is from the various cooling systems. Source water is reduced
by cold lime softening prior to use. The spent lime from this process
is currently land applied onto local farmland.
Waste streams generated on site include cooling tower blowdown which
is relatively high in orthophosphates - up to 15 mg/L - that need to be
reduced to less than 2.5 mg/L (1 mg/L as phosphorus) prior to discharge
back to the Red Deer River.
A detailed bench scale and follow-up pilot scale program was undertaken
to evaluate phosphorus removal by chemical coagulation using the spent
lime from the water treatment process as a source of alkalinity and an
aid to coagulation.
This paper will discuss the rational for looking at this and various
other chemical combinations to address this problem, and will present
the full results of the investigation. The impact of waste stream characteristics
variability are discussed. Limited success was achieved at ambient pH.
A high pH process, which relied on achieving optimal pH of 10.5 for precipitation
of phosphorus was more successful and produced a settleable floc. In either
case the addition of spent lime was beneficial to the process in reducing
phosphorus levels and also reducing coagulant dose.
The success of this technology could see its potential application to
municipal utilities that practise cold lime softening and need to address
phosphorus removal at their wastewater plant.
KEYWORDS - Wastewater, Phosphorus, Chemical Coagulation, Clarification,
Lime Sludge, Orthophosphates
INTRODUCTION
Preface
This paper presents the findings of a pilot and bench study that evaluated
phosphate removal from cooling water blowdown. The study was conducted
by Associated Engineering and Infilco Degremont Inc. (IDI) from April
to August, 1998 at the NOVA Chemicals Ltd. plant located near Joffre,
Alberta. The study evaluated the use of a
Degremont Densadeg clarifier for phosphate removal and established design
criteria for a proposed phosphate removal plant.
The need for phosphate removal is found in Alberta Environmental Protection's
(AEP) Standards and Guidelines for Waterworks, Wastewater and Storm Drainage
Systems, 1997, which states that effluent discharged to water bodies must
contain less than the maximum allowable concentration of 1.0 mg/L phosphorus
(equivalent to 3.0 mg/L total phosphate). This is the most stringent phosphorus
limit in the guidelines and applies to municipalities with population
greater than 20,000. NOVA Chemicals Ltd. have committed to meeting this
performance standard.
Background
The NOVA Chemicals Ltd. Joffre Plant is presently undergoing an expansion.
The existing cooling towers, which serve E1 and E2, each have different
chemical treatment programs. These programs include the addition of phosphates
to reduce fouling and deposition of unwanted impurities in the cooling
water process stream. The expansion includes the construction of several
additional cooling towers which will increase effluent discharge along
with phosphate loadings.
Scope of Study
The most important clarification design variable to be evaluated was the
rise rate, as this would determine the overall size of the clarifiers.
Additional objectives of the study were to:
- Verify, at a pilot plant scale, optimum chemical dosages determined
in the bench scale study.
- Determine lowest achievable phosphate levels in cooling water blowdown.
- Evaluate both alum and ferric chloride as coagulants.
- Evaluate various types of polymers.
- Determine optimal spent lime concentrations (volumetric and gravimetric).
- Analyse solids concentrations throughout the process for design and
operational guidelines.
- Analyse the effluent on site and at a certified laboratory to compare
and verify results.
- Analyse sludge from the various processes for metals and nutrients.
- Determine need for filtration of phosphate effluent and optimal filtration
rates and media types.
- Perform jar tests using similar processes utilized in the Densadeg
clarifier.
- Perform jar tests simulating the addition of LAO, a waste product
from the proposed AMOCO processing plant.
Note: Phosphorus levels in this paper are expressed as phosphate, where
1 mg/L of phosphorus is equivalent to 3 mg/L of phosphate (PO4). Total
phosphate to orthophosphate ratio is discussed later.
EQUIPMENT
AND METHODS
Pilot Plant Equipment
Figure 1 is a schematic of the pilot plant. The pilot plant consisted
of a 22.5 m3/hr Densadeg clarifier followed by two filtration units. The
clarifier consisted of a flash mixer/flocculator, reactor vessel and a
thickener/clarifier vessel. Coagulant was injected at the flash mixer/flocculator,
while spent lime, fresh lime and polymer was added at the reactor vessel.
The reactor vessel also received recycled sludge from the thickener/clarifier
vessel. Supernatant from the thickener/clarifier vessel flowed up through
tube settlers to be collected in launders and gravity fed to two clear
acrylic filters, Filters #1 and #2 on Figure 1. The clear filters allowed
for visual inspection of the clarified effluent. Each filter contained
the same type of media and configuration, as indicated in Table 1. The
two filters were operated at different filtration rates.
Table 1. Filter Media Configuration
|
Filter Number |
Description |
| Filter #1 & 2 |
300 mm of
0.5 mm effective size sand
300 mm of 1.0 mm effective size anthracite |
Figure 1. Pilot Plant Flow Diagram
(click image for more detailed figure)
The on-line analytical instrumentation used for monitoring water quality
parameters consisted of a Hach turbidity meter, Wika head loss sensors,
a Hach pH analyser, and a flow meter.
Coagulants And Polymers
The coagulants and polymers used were as follows:
- Aluminum Sulphate 49% active and SG of 1.3
|
Reported as active ingredient mg/L |
- Ferric Chloride 49% active and SG of 1.34
|
Reported as active ingredient mg/L |
- Liquipam 452 long chained cationic polymer
|
Reported as neat |
- Jaschem A305 anionic polymer
|
Reported as neat |
- Nalco 8103 cationic polymer
|
Reported as neat |
- Betz 1115L cationic polymer
|
Reported as neat |
Polymers were allowed to age for minimum of one hour before dosing. Maximum
age of polymers used in the study was five days.
Aluminum sulphate and ferric chloride was dosed as mg/L active chemical
where 100 mg/L (active) would equal 100/(0.49*1.34)=152 mg/L of neat chemical.
All other chemicals were dosed as neat, also known as wet.
THE
STUDY
The characteristics of the E1 cooling tower and E2 cooling tower blowdown
waters differed greatly in alkalinity, pH, concentration and type of phosphate
because different chemical treatment programs are used in each, see Table
2. Therefore, the type of process required to remove phosphate differed
for each of the effluent streams to provide adequate flexibility it is
desirable that the phosphate removal process be able to treat any combination
of effluent streams. The three blowdown streams used in the analysis of
the treatment processes were:
- E1 blowdown water
- E2 blowdown water
- A blend of 1/3 E1 blowdown water and 2/3 E2 blowdown water
Table 2. Cooling Water
Blowdown Characteristics
| |
E1 Blowdown |
E2 Blowdown |
| Calcium |
750 |
650 |
| Turbidity (NTU) |
16 |
6 |
| OPO4 |
14 |
6 |
| pH (units) |
7.1 |
8.6 |
| M. Alkalinity as CaCO3 |
35 |
270 |
| Total Hardness as CaCO3 |
1300 |
1100 |
mg/L unless otherwise stated
The study focused on two main processes, a high and a low pH treatment
both of which has shown promise during an initial bench scale study.
| |
Low pH process |
|
High pH process |
|
160 mg/L of coagulant |
|
160 mg/L of coagulant |
|
2 mg/L of polymer |
|
2 mg/L of polymer |
|
1 to 2 % spent lime |
|
200 to 500 mg/L of lime |
|
|
|
1 to 2 % spent lime |
Lime dosage varied due to the different buffering capacities of El and
E2 blowdown water. The high alkalinity E2 blowdown water required greater
dosages of lime than E1 blowdown water in order to maintain the same pH.
In order to meet the AEP maximum allowable concentration of 1 mg/L phosphorous
(3 mg/L total phosphate), an orthophosphate concentration of 1.5 mg/L
was targeted. This target concentration was determined based on analyses
conducted during Associated Engineering's "Phosphate Removal Study".
On the basis of 15 samples that were sent to a certified lab, it was determined
that the average ratio of orthophosphate to total phosphate was 0.835.
Therefore, 3.0 mg/L total phosphate equates to 2.5 mg/L orthophosphate.
A target concentration of 1.5 mg/L provides a degree of safety of 1.0
mg/L.
Discussion
Table 3 summarizes the results of all the jar tests, the Associated Engineering
pilot plant, and the Densadeg clarifier operation. The successful processes
are indicated with a yes (Y) while the unsuccessful processes are indicated
with an No (N). For a process to be successful, not only must the target
orthophosphate level of 1.5 mg/L be met, but the minimal acceptable rise
rate of 12.8 m/hr must be met and sludge production must be less than
5% by volume.
Table 3. Summary of Phosphate
Removal Processes
|
Stream |
Study |
Process |
Alum |
Alum, Spent Lime |
Alum, Lime |
Alum, Lime, Spent Lime |
|
E1 Blowdown |
Bench Scale |
97 Jar Test PO4 |
N |
X |
|
Y |
| 98 Jar Test PO4 |
|
Y |
Y |
Y |
| 97 Pilot PO4 |
|
|
|
|
|
Densadeg |
Clarified PO4 |
|
N |
Y |
Y |
| Rise Rate |
|
Y |
N |
Y |
| Sludge |
|
Y |
N |
Y |
| Filtered PO4 |
|
Y |
Y |
Y |
|
E2 Blowdown |
Bench Scale |
97 Jar Test PO4 |
|
Y |
|
Y |
| 98 Jar Test PO4 |
Y |
Y |
Y |
Y |
| 97 Pilot PO4 |
|
|
|
|
|
Densadeg |
Clarified PO4 |
Y |
N |
|
Y |
| Rise Rate |
Y |
N |
|
Y |
| Sludge |
Y |
Y |
|
Y |
| Filtered PO4 |
Y |
N |
|
Y |
|
E1 E2 Blowdown |
Bench Scale |
97 Jar Test PO4 |
N |
N |
|
Y |
| 98 Jar Test PO4 |
N |
N |
|
Y |
| 97 Pilot PO4 |
|
Y |
|
Y |
|
Densadeg |
Clarified PO4 |
|
N |
|
Y |
| Rise Rate |
|
N |
|
Y |
| Sludge |
|
Y |
|
Y |
| Filtered PO4 |
|
Y |
|
Y |
Discussion of Results. By far the most successful treatment was
the high pH process. This
process met orthophosphate target level, the sludge production limitation
and the required rise rate for all effluent streams. The low pH process
using alum alone, successfully treated E2 blowdown water during the initial
parts of the study. However, due to cooling tower process upsets, E2 blowdown
water was much more difficult to treat in the latter parts of the study
and required the high pH treatment process.
Equipment Performance
The Densadeg clarifier met the target rise rate of 12.8 m/hr which is
about three times greater than typical solids contact clarifiers. The
greater rise rate for the Densadeg clarifier can be attributed in part
to the thickening process in which controlled amounts of sludge are recirculated
from the thickener/clarifier vessel into the reactor vessel. This leads
to an increase in particle size and weight. Settling velocity will therefore
increase based on Stokes' law which states that settling velocity is proportional
to particle size and weight. Other factors allowing for higher settling
rates are as follows:
- No energy is transferred from the thickener/clarifier turbine to the
sedimentation zone. In a normal solids contact unit, energy from the
turbine could suspend a sludge blanket.
- The flow does not pass through the concentrated portion of the sludge.
This too prevents sludge blanket suspension.
- Tubes settlers and baffled plates assist in the sedimentation process.
One potential disadvantage to the Densadeg clarifier is increased maintenance
due to the additional sludge recirculation pump. As well, it was found
in the pilot study that the Densadeg clarifier was unable to thicken magnesium
hydroxide sludge, but then it is unlikely that any thickener would be
able to thicken the same sludge without chemical addition.
Process Challenges
Spikes in hydrocarbon concentration in the blowdown water led to difficulties
in meeting the treatment requirements. Hydrocarbon concentrations can
build up as the cooling water flows through the heat exchangers. In order
to meet treatment requirements, the high pH process was required during
periods of increased hydrocarbon concentration.
During the course of this pilot study, blowdown flows occasionally dropped
to a small percentage of the proposed design capacity. During cooling
tower maintenance, the flow dropped as low as 5% of the proposed design
capacity. Even with all the towers in operation, the flows dropped to
as low as 10%. Therefore, adequate turn-down capability should be provided.
The most significant process upset that occurred during the pilot study
was the precipitation of magnesium hydroxide, Mg(OH)2. Magnesium hydroxide
is a low density floc with poor settling properties that results from
the removal of magnesium hardness.
Normally when the pH is elevated, addition of lime will remove calcium
hardness as calcium carbonate as the primary reaction and magnesium hardness
removal will occur to a lesser extent. The calcium carbonate attaches
to the lighter magnesium hydroxide floc and assists in settling. However,
presence of anti-scaling agents in the blowdown water prevented the precipitation
of calcium carbonate.
By inhibiting the precipitation of calcium carbonate, the presence of
anti-scaling agents led to greater magnesium hydroxide production. As
well, the problem of increased magnesium hydroxide was compounded by the
absence of any calcium carbonate to improve the settling properties. It
was found during the operation of the Densadeg pilot plant that when more
than 200 mg/L of magnesium hardness was removed the following problems
were observed:
- Large quantities of sludge were produced, which increased sludge levels
within the sedimentation zone up to three metres.
- Increased quantities of sludge were blown down.
- Target rise rates of 12.8 m/hr could not be met. If flow was increased,
sludge would pass through the sedimentation zone along with the supernatant.
- Volumetric sludge concentrations within the reactor increased to 23%
as compared to the normal 10%.
- Ten minute volume over volume values which determines concentration
and thickening properties was recorded at an average of 91%.
With the high magnesium hydroxide precipitation, it was found that colour
and phosphate removal increased. However, when considering the above process
problems, the excessive precipitation of magnesium hydroxide should be
mitigated. During the pilot study, spent lime was added and pH was slightly
reduced to mitigate these problems.
Coagulants And Polymers
The pilot study investigated coagulants which would lead to the precipitation
of phosphate as a metallic compound. Two types of coagulants were dosed
to the various streams, aluminum sulphate (alum) and ferric chloride.
It was important to pilot with ferric chloride in the phosphate removal
process since this was the optimal coagulant in the softening process.
If it was found that ferric chloride worked reasonably well in the phosphate
removal process this would eliminate the need for two types of coagulants
on site.
The following results were observed from the pilot study:
- Alum showed better results than ferric chloride with regard to turbidity
removal.
- Aluminum residuals with the use of alum averaged 0.14 mg/L.
- Iron residuals with the use of ferric chloride averaged 0.36 mg/L.
- Iron residuals decreased as pH increased.
LIME
Lime dosages varied due to the different buffering capacities of the blow
down streams. The high alkalinity blow down water required greater dosages
of lime than low alkalinity blowdown water in order to achieve the same
pH.
Figure 2. Phosphate Removal as a Function
of pH
Phosphate removal was dependant on pH. Figure 2 presents the results
from the pilot study along with results from a study published by Albertson
and Sherwood in 1967.
Spent Lime
Spent lime was obtained from the blowdown line of the existing process
water softeners and pumped to the Densadeg pilot plant. The consistency
of the spent lime varied due to the dilution from back flush water entering
the blowdown system. The average total solids content of the spent lime
was determined to be 20%.
Metering of the spent lime at exact concentrations was difficult to achieve.
At 20% solids and high hose pump speeds the hose on the suction side of
the pump would collapse or the abrasive nature of spent lime would cause
hose failure. A progressive cavity pump was also used to meter the spent
lime; this failed due to stator wear. Metering by gravity and controlling
flow using a valve and rotameter also proved to be inconsistent.
Due to difficulty in metering spent lime, the study team was asked to
determine a reasonable solids content of spent lime at which it could
be metered. Known concentrations of sludge were diluted to a consistency
similar to sludge which could be metered, based on experience. It was
determined that the spent lime should be diluted to 10 to 15% solids for
metering. As spent lime concentrations from Densadeg clarifiers can reach
30%, a dilution factor of three would be appropriate.
Figure 3. Phosphate Removal with Spent Lime
Because of the difficulties experienced in feeding spent lime, it was
eliminated from the pilot plant process for a while. This resulted in
process failure. Spent lime serves two purposes in the treatment of phosphate
removal; it assists in the adsorption of phosphate, and is used as a weighting
agent in the sedimentation process that enables light floc, such as Mg(OH)2,
to settle. Figure 3 illustrates the phosphate adsorption capacity of spent
lime at various spent lime dosages, without coagulant or polymer addition.
Throughout this study it was found that the required spent lime dosage
for phosphate removal was approximately 1 to 2% by volume. The precise
dosages of spent lime could not be determined.
The availability of spent lime is dependent on the calcium removal in
the process water softeners and the flow through these softeners. The
available concentration of spent lime which could be metered to the proposed
phosphate removal plant will then be a function of the ratio of blowdown
water to softened water. This ratio will be affected by the amount of
drift from the cooling towers. As drift increases less blowdown is required.
Therefore, an increase in drift results in greater concentrations of available
spent lime. Table 4 compares the available spent lime concentrations as
a function of the above ratio. The calculations were based on the following
assumptions:
- raw water calcium 120 mg/L
- softened water calcium 30 mg/L
- calcium carbonate production 90 mg/L
- sludge composition: 95% calcium carbonate
- spent lime total solids: 20%
Softened Water to Blowdown Ratio
Available Spent Lime % Qin
Table 4. Spent Lime Availability
|
Softened Water to Blowdown Ratio |
Available Spent Lime % Qin |
|
6 to 1 |
0.56% |
|
8 to 1 |
0.75% |
|
10 to 1 |
0.95% |
|
12 to 1 |
1.13% |
|
15 to 1 |
1.4% |
|
20 to 1 |
1.9% |
Qin=Blowdown Flow
It should be noted that NOVA Chemicals Ltd are actively pursuing drift
mitigating measures at the plant site. This will result in blowdown water
quantities increasing.
Extraction Sludge
The Densadeg clarifier is designed to produce extraction sludge that is
high in solids. Sludge was sampled on seven occasions and sent to a lab
for analysis. The highest concentration achieved was 32%. At this concentration
the extraction sludge had difficulty flowing through the discharge lines.
Sludge was gravity fed into a holding tank and then pumped into a mud
tank. At this concentration the sludge pumps operated at a fraction of
their capacity.
The sludge from the phosphate removal process was analysed for ICP metals
and the important metals are listed in Table 5:
Table 5. Extraction Sludge
Analysis
|
Blowdown Source |
E1 |
E2 |
E1/E2 |
| Suspended Solids (mg/L) |
100,000 |
113,000 |
193,000 |
| Total Organic Carbon (mg/L) |
357 |
48.5 |
-- |
| Arsenic (mg/L) |
0.43 |
0.02 |
2.2 |
| Iron (mg/L) |
29.8 |
0.002 |
152 |
| Calcium (mg/L) |
30,700 |
298 |
81,400 |
| Magnesium (mg/L) |
2,510 |
49.5 |
8,020 |
The sludge contains high levels of nutrients, which provides an excellent
food source for microbes and algae. Samples of sludge were collected and
within one week a variety of biological growths were present. It was also
observed that sludge within the tanks went septic within a short period
of time; indicative of potential problems with algae growth and odours.
For this reason, on-site sludge dewatering should be considered when sludge
cannot be immediately disposed of to land application.
Filtration Study
The effluent from the Densadeg was filtered through pilot scale filters
at various filtration rates from 5 to 15 m/hr. Turbidity and head loss
was monitored continuously while phosphate concentrations were determined
by grab samples. The general objective of the study was to determine filter
run times and phosphate removal at various filtration rates. Specific
objectives of the study were to determine if the high pH process can be
replaced with the low pH process plus filtration, and to determine clarified
and filtered water characteristics during times of upset.
Ten combinations of blowdown stream, treatment process and chemical treatment
were piloted. The results of these combinations are presented in Table
6 which shows clarification alone could not meet the phosphate target
level in five of the processes. By filtering the clarified effluent three
of these five processes then met the phosphate target levels. As well,
three processes that met the average phosphate target level after clarification,
had experienced phosphate concentration spikes that exceeded target levels
but the spikes were removed through filtration.
Two of the three processes that met phosphate target levels with filtration,
but not with clarification, were low pH processes. This indicates that
generally a high pH process could be replaced with a low pH process plus
filtration. A high pH process would be needed only when blowdown water
is more difficult to treat.
The average filtration run times, specific filtration run volumes, and
average phosphate removal rates are shown in Table 7. The average run
times for filtration rates of 5, 10, and 15 m/hr were 11, 6.75, and 3.8
hours respectively. The largest specific run volume, 67.5 m3/m2, corresponded
to a filtration rate of 10 m/hr. In terms of performance, filtration rates
of 5 and 10 m/hr averaged 27% phosphate removal, while at 15 m/hr the
average phosphate removal dropped to 22%. The choice of filtration rate
will depend on economics and the degree of safety required.
Table 6. Summary of Filtration Study
|
Test # |
pH |
Chemicals |
Clarified OPO4 (mg/L) |
Filtered OPO4 (mg/L) |
% Reduction thru Filters |
|
E1 Blowdown |
|
2 |
High |
ALP |
0.9 |
0.4 |
55 |
|
3 |
Low |
ASP |
2.1 |
1.4 |
33 |
|
4 |
High |
ASLP |
1.0 |
0.8 |
20 |
|
5 |
High |
FSLP |
2.3 |
1.1 |
52 |
|
6 |
Low |
FSP |
2.8 |
1.2 |
57 |
|
E2 Blowdown |
|
1 |
Low |
AP |
0.7 |
0.3 |
57 |
|
7 |
Low |
ASP |
3.1 |
2.8 |
10 |
|
E1/E2 Blowdown |
|
9 |
High |
ASLP |
1.0 |
0.7 |
30 |
|
10 |
Low |
ASP |
3.7 |
2.3 |
38 |
|
Failed to meet 1.5 mg/L goal. |
| A= Alum, F=Ferric Chloride,
S=Spent Lime, L=Fresh Lime, P=Polymer |
Table 7. Comparison of Filtration
Rates
|
Filtration Rate |
5 m/hr |
10 m/hr |
15 m/hr |
| Run Time (hours) |
11 |
6.75 |
3.8 |
| Specific Filtration Run Volume
(m3/m2) |
55 |
67.5 |
57 |
| Average Phosphate Removal (%) |
27 |
27 |
22 |
SUMMARY
The pilot study was successful in meeting the objectives set out in the
scope of work. Optimal processes were identified along with design criteria
for the proposed phosphate removal plant. The conclusions are as follows:
- The high pH process showed the best results regarding phosphate removal,
minimal sludge production, and rise rate. The target phosphate concentration
of 1.5 mg/L orthophosphate the target volumetric sludge production of
5 %, and the target rise rate of 12.6 m/hr were all met.
- The use of spent lime proved beneficial in the removal of phosphate,
increased settling rates and improved sludge thickening. The elimination
of spent lime led to process failure. Process failure included large
volumes of magnesium hydroxide sludge and low settling rates.
- The metering of spent lime was difficult to achieve.
- The optimal spent lime dosage is 1 to 2%, however the production of
spent lime in the softeners is approximately 1%. This percentage will
increase as drift increases.
- E1 blowdown water required a more vigorous high pH treatment process
compared to E2 blowdown water.
- During the initial part of the study, only alum and polymer were required
to reduce phosphate concentrations to below target levels in E2 blowdown
water. However, due to cooling tower upsets, the high pH treatment was
required during the latter part of the study.
- Alum as a coagulant resulted in lower turbidity as compared to ferric
chloride. Also, metal residual concentrations were lower with alum.
- The Densadeg clarifier thickened the extraction sludge up to 32%,
which will require dilution to achieve pumpable sludge.
- The extraction sludge contained high levels of nutrients, which provide
an excellent food source for microbes and algae. It was observed that
the extraction sludge in the holding tanks and sample containers went
septic within a short period of time.
- Softening of the blowdown water was inhibited by the presence of anti-
scaling agents.
- The use of filters further reduced phosphate levels by an average
of 27%. Filtration also reduced phosphate to target levels in three
of the five processes where clarified effluent did not meet target levels.
- At filtration rates of 5 and 10 m/hr, phosphate removal was not significantly
different; corresponding filter runs were 11 to 6.75 hours. When the
rate was further increased to 15 m/hr, filter run times dropped to 3.8
hours and average phosphate reduction dropped to 22%. The maximum specific
filter run volume was 67.5 m3/m2, at 10 m/hr filtration rate.
ACKNOWLEDGEMENTS
The following personnel are acknowledged for their respective contributions
to this study:
- Nandan Vani, P.E., Bantrel Inc., Environmental Engineer, who developed
the study programme.
- C.J. Lee, P.Eng., NOVA Chemicals Ltd., Process/Environmental Engineer,
who directed and managed the programme.
The author is indebted to these people for their guidance and contribution
to this paper.
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